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Pinning table improvement, Summaries of Engineering

To increase fabric consumption

Typology: Summaries

2020/2021

Uploaded on 02/22/2023

hasan-nufais
hasan-nufais 🇮🇳

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REDUCE THE FABRIC CONSUMPTION BY
IMPLEMENTATION OF PROPER PINNING
PROCESS AS PER SOP
BY
HASAN NUFAIS M L
PROJECT INTERN TRAINEE
GUIDED BY
Mr. JAYAKUMAR PALLATH MENTORED BY
Mr. GANDHI GANESHAN
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REDUCE THE FABRIC CONSUMPTION BY

IMPLEMENTATION OF PROPER PINNING

PROCESS AS PER SOP

BY

HASAN NUFAIS M L

PROJECT INTERN TRAINEE

GUIDED BY

Mr. JAYAKUMAR PALLATH

MENTORED BY

Mr. GANDHI GANESHAN

PROJECT GANTT CHART ACTIVITY/TIME LINE February March APRIL 3rd week 4th week 1st week 2nd week 3rd week 4th week 1st week EGL Process flow from "store to cutting"study study on Importance of Pinning Process in EGL Trouble shoot the pinning table Collection of past consumption data for fabrics Analysis of Avg consumption for different fabrics PIN IT software training to Marker makers Study on where the most fabric wastage occurs Lterature study for the solution to the problem Brainstorming the importance of PIN IT Software Implement the new plan Brainstorming the operators about the new plan Data collection& result analysis for the implemented process Power point Presentation

OBJECTIVES OF THE PROJECT

 To study on current cutting process in EGL

 To identify the methods to reduce fabric wastage in cutting

 To implement the methods identified

 To analyze the final results

METHODOLOGY Study on Current process

  • (^) Observation of Laying in EGL
  • (^) Observation of Laying for Checked & Striped Fabrics Problem identification in current process - (^) Fabric wastage is more - (^) More Relaying Implement new process &Validate the results - (^) Made Pinning marker & reduce in fabric consumption - (^) Proper use of PIN IT Software

FABRIC CONSUMPTION ANALYSIS CHECK FABRIC PINNING MARKER

  • (^) Marker buffer =5mm
  • (^) Utilization = 79.26%
  • (^) Consumption =140cm

FABRIC UTILIZATION BEFORE

Not using Pinning

Table For checks

1. PIN IT software is not properly

utilized.

3. Operators didn’t follow the PIN IT

sheet.

4. The process of SOP for Pinning is

not at all followed

5. Marker buffer is more

Line matching

is not there

Cutting Process Flow for

Checks & Stripes without

Proper Pinning

Cutting Process flow for

Checks & Stripes with

Pinning

Ready Cut Line Matching & Relaying Block Cut

Laying

Marker planning

Fabric received from store

Ready Cut Pinning & Laying with Line matching Marker Planning Fabric received from the store Benefits:

  • (^) Proper Pinning Process as per SOP
  • (^) Line Matching of Fabrics
  • (^) Relay Operators Can be reduced
  • (^) Time saving and Quality improvement

S.N

O

CAUSES REASON STEPS TAKEN TO

RESOLVE

IMPROVEMENTS AUTHORIZED

PERSON

1 Pins and Pin holder were damaged and Blunt & Insufficient use of PIN IT Software Improper maintenance of Pin Table

  • Request maintenance team to trouble shoot the table
  • Empty needle bar Pins has been changed - Improved performance of Pin table - Material handling became easy for Operators Mr. Maruthi 2 PIN Software &PIN sheet has not been followed and Pins were set by using Marker Lack of awareness about PIN IT Software& not been used
  • PIN IT Software training has been given to CAD People
  • Given awareness to the operator about the PIN sheet
  • PIN IT software has been utilized
  • PIN sheet has been followed for pinning work order Mr. Raja 3 Line matching for checks & stripes are not Proper SOP for Pinning and PIN sheet has not been followed
  • SOP is followed for before & after Marker making
  • Repeat size has been checked as per SOP and based on that PIN sheet has been issued
  • Fabric consumption has been reduced
  • Fabric Parts has been Ready cutted Mr. Sampath, Mr. Narayanan

SAVING OF COST AND MANPOWER REDUCTION Man power reduction

  • (^) Relay operators reduction in batch processing ( 4 operators to 2 operators ).
  • (^) Ready cut of lays
  • (^) Improved quality of garments.
  • (^) Fabrics on an average 2-3cm can be saved
  • (^) PIN table target = 800pcs/day
  • (^) Fabric savings Per table= 800*3= 2400cm /table